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The rear bumper that was donated had no mounting bracket, just 2 coach bolts, so I needed to fabricate new brackets
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Had some plate left over, so cut 2 pieces and welded them together
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Welded 2 captive nuts onto each bracket
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knowing it would upset too many of you if I didnt, I sprayed the new brackets biggrin.gif
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Fixed the bracket to the bumper
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Then fixed the brackets to the car. I think even Karl would admit this one needs some `back to black` tongue.gif
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Louise spent the best part of the day removing wheels, adjusting the coil overs, refitting the wheels, then removing them again when I said it was at the wrong height !
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I found why the brake pedal was `spongy`, it wasn't air, but a brake union that wasn't quite tight enough and was weeping.. Another 1/2 turn and it was secure and the brakes were firm again .
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Sprayed the rest of the cage and fitted that
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Tacked the door bars into position and then my welder overheated. Kind of summed up my day really...
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Another hectic day, but it went well I think.

Fitted the front grille
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Still need the strip that goes at the bottom...  Next job was the Horn. Found this broken wire once I stripped back some of the outer black covering
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Fixed that but it still didn't work. Spent about 30 minutes trying to find the break, eventually, I just ran a new fused feed from a supply under the engine bay
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Tidied up all the wiring and now have working horn
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Next job was the bloody exhaust. I`ve decided, I hate working on exhausts....
The first silencer and flexible joint was hanging too low. I`m not sure if the down pipe was bent in the crash, but it seems to be pointing downwards instead of towards the back of the car
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Removed the exhaust. (sounds so easy when I type it. took about 45 minutes of cursing...)
I know the flexible joint can be moved, but I wanted to angle the pipe slightly too. By using a blunt chisel, I was able to put a crease in half of the pipe which caused a slight bend .
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Crease and a slight bend in the previously straight flexible coupling
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There was no exhaust mount near this section, so cut a piece of sheet steel, Bent it and drilled a couple of holes
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Then secured it to the underside of the gear lever, used a jubilee clip and exhaust rubber to support the section of exhaust
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The refitted system, still not brilliant, but better than it was.. It doesn't look it from the photos, but its now about 7mm higher than before...
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Sprayed the door bars and roll cage. Didn't have time to fit the top of the X, I`ll do it IF I get time before Friday, but its not looking likely... Cage and bars look good I think
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The window winder was hitting the roll cage, I couldn't lower the window without opening to door..
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Removed the handle and drilled out the spinning part
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Shortened the `arm
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Re drilled and fitted a new handle with locknuts I can now operate the window with the door closed thumb.gif ( I did cut off that long bit of thread too...)
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I refitted the seats and harnesses.
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Louise gave the inside of the car a good wipe down to remove all the dust I'd made when grinding / welding.
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Matthew refitted the sunvisors
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Started the car and with the bonnet closed, the bonnet was vibrating slightly, opening it and found this wear mark
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It is from the throttle cable mount, I can cut out part of the box section on the bonnet, I had to do it on my old golf too. Also had a slight rubbing of the air intake pipe into. Lou & Mat have shown the offending points here .
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May 21st.

4x New Paradas fitted, lets see how they go next week. If the forecast rain appears, they will not be doing many laps, thats for certain...
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I've read many people say you need a bit of string, 2 people and some washing up liquid to change a window / windscreen, but couldn't find a how-to (watch loads of people post links now ), anyway, in true DIY style, I made my own. I'd never done it before, but it was surprisingly easy. I did the guide for a rear quarter window, its exactly the same principal for the rear screen and windscreen, but as they need 2 hands, I couldn't hold the camera as well .

To remove the old window, simply press firmly on one corner and maintain the pressure,
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you will SLOWLY see the rubber start to `unfurl` and loosen its hold on the glass
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Maintaining pressure move your hand along the glass and allow the rubber to unfold at its own speen, DO NOT FORCE IT, it will take time.
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When the top edge is complete, the screen will `fall out`, have the second person take the weight, allow the rubber to unfurl down the edges and lift out the glass
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Lift the glass clear and place to one side
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REFITTING

Using a length of STRONG twine, press it into the rubber, where the metal will eventually sit, I used a flat bladed screwdriver to push the string to the bottom and to aid fitting, dragging the screwdriver along pressed the string in much faster
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Leave 12" lengths overlapping at one corner
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Using diluted washing up liquid / water mix, thoroughly lubricate the slot with the string and the inside rubber edge
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I'm not sure if this next bit is the correct way, but it seemed to work well for us. I put the bottom corner in place and made sure the rubber sat properly, inside and out
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Next, whilst the person outside puts LIGHT pressure on the glass, the person inside pulls the string horizontally away from the glass. This is the bit where the string deforms the rubber and causes it to fit over the metal .
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Slowly work your way along the top edge of the glass
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Continue along the top
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Now, have a look from the outside and check the rubber lines up with the marks on the paint from before, I needed to push the whole pane of glass slightly towards one side to make it `sit` properly in the groove, its obvious if not, the string becomes much harder to pull. Continue pulling the string. If you find it difficult, try pulling the other end and working from the opposite direction, by doing that I found it went in easily
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And that's it, we did the first window in under 10 minutes ohmy.gif Both rear quarters, rear screen AND windscreen in 30 minutes ! That was with us taking our time as it was our first attempt. It was far easier than expected

Windscreen before (it had a small crack in the drivers line of vision)
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`new` one fitted (was the 5 week old one from my old car...)
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Fabricated some mounts for the radiator and fan.
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Tried to open the bonnet and it wouldnt open, had a look and saw the cable had popped out of the slot
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Some gaffer tape and a securing cable tie did the trick
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I`d noticed the oil temp on the MFA had stopped working. a 15 second diagnosis was all that was required. :-)
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refitted the connection and all was well again.
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The oil breather pipe from the engine goes into the airbox
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'A popular mod that people seem to do is fit an oil catch tank, so any oil that is blown down the pipe is collected, rather than going back to be reburned in the engine.'
Simply find a suitable plastic bottle, remove the pipe from the airbox and fit to the top of the bottle. Make some holes in the bottle to allow it to breathe and secure the pipe into the bottle neck. Ensure you block the inlet to the airbox where the pipe used to go...
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To ensure no oil sprayed out of the vent holes, I placed some oil absorbent matting over the top as a filter
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Then place the bottle in a suitable place that is secure and I then cable tied it into place
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May 24th

The front nearside brake was still catching, so I removed the carrier and filed down the contact points slightly in case the pad was not sliding freely
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'It made no difference, I was still getting the front left sticking and getting hot, that meant that when I braked hard, that pad was already at full temp and was braking better than the drivers front, causing me to not brake in a straight line . That combined with the rears still locking under extreme braking meant for zero confidence in my brakes. '

Thought I had better take a look, removed the front caliper, blocked the fluid inlet with a bit of old brake pipe with the end bashed flat. Used a foot pump via the bleed nipple to push the piston out of the cylinder, the hammer handle is to stop the piston shooting out.
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piston removed from caliper
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its in pretty good condition, but had a couple of `nicks`. I`ve had them much worse, so was a little suprised how clean this looked !
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polished it with some fine wire wool
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fitted the new bore seal
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after fitting the dust seal carefully push the cylinder squarely into the bore
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Used the opportunity to fit the new blue stuff pads
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did the rears at the same time, used the caliper rewind tool to push the cylinder back
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New rear pads fitted
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Bled the brakes and went for a short run to bed them in.

You may remember the bumper was not exactly `black`...Louise applied some superb cheap back to black substitute
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The finished result
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'And the front for comparison. I have only washed it, not had time to give it a coat of polish. I think it looks pretty good now. I'll be fitting the `missing` strip at the bottom of the grille in Germany.'


Conclusion.

The car was completed with hours to spare before the Ferry to back to the Nurburgring, a truly epic build that Nigel, his Wife, Son and Daughter should all be proud off. Since then, the car has put in some excellent laps at the Ring, and has not missed a beat. Congratulations Nigel, Fastclassics Salutes you! 

Please visit Northloop.co.uk for the best English speaking Nurburgring community on the web!



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